Trip Report
June 13, 1962
Reference
4-7000-XXXX
To:
XXX
From:
L. H. Williams
cc
D. J E
Al Hobbs
L. C. M
J. E. Long
J. H. H
J. H. H
V. M.
W. B. A
S. D. H
B. D. P
W. W. R
H. C. H
H. L. B
Subject: Turbine Race Car Trip Report, Indianapolis Speedway
The following report covers the period from April 12 to
May 25. During this period, the John Zink Trackburner race car was completed and
shakedown tests were made in Tulsa, Oklahoma. The car was transported to the
Indianapolis Motor Speedway where it attempted and failed to turn lap speeds
sufficiently high to enter the 1962 Memorial Day Race.
On my arrival in Tulsa, the car consisted of' little
more than the chassis and assorted suspension parts. The detail design and
construction of the car was done by Chief Mechanic Denny Moore. The major delay was the
construction of the fuel tanks, which were hand built and form fitted to the
chassis. The tanks internal plumbing was extremely complicated to insure their
complete filling with pressurized fuel. Until the tanks were completed very
little could be done on the chassis, body, or suspension.
The tanks were completed April 18. Final assembly of the car began April 2l
and the engine made its first start on April 25.
The chassis is of space frame construction, uses 4130, 1-1/4 diameter, .083
tubing. All welding is done by heli-arc. The bare chassis weighed 127 lbs. The
suspension is independent all around and manufactured by Troutman Barnes.
"A" frames in front and single arms with 4-foot radius rods in the
rear. Girling disk brakes were used, outboard in front and inboard at the rear.
Braking was approximately 60% rear and 40% front.
The fuel tanks were constructed of aluminum and covered with fiberglass.
Total capacity for the two tanks was 63 gallons. Each tank weighed 40 lbs
The steering was rack and pinion with an 8 to 1 ratio,
Page 2
Monroe shocks were used front and rear and were also used to support the coil
spring suspension.
The engine was direct connected to the Halibrand quick-change rear end. See
drawing 44-2501. No clutch or transmission was used. The quick-change was
connected to the rear wheels with a pair of Mechanics universal shaft
assemblies. Two .125 inch stainless plates were installed in the frame on either
side of the second stage wheel in the event of a wheel burst. This was in
addition to the burst shield provided by Boeing.
The wheels were 16 inch magnesium. 7.80 X 16 Firestone Speedway tires were
used in the rear and 7.00 X 16 in front. Tire pressure was +/- 40 psi. The car
weighed 1200 lbs. Dry with 63% of the weight on the drive wheels. This compares
to 1600-1650 lbs. for a conventional roadster. The wheelbase was 102 inches.
Front and rear tread was 52.5 inches.
Photos of the car showing internal and external details are available.
Following the initial start, the next two days were spent with shakedown runs
at the John Zink ranch. Mister Zink has his own 5/8 mile track with a turn
radius of 225 feet and 11 degree banking comparable to the turns at the Speedway. Quite a few
interferences and troubles were uncovered and corrected during these two day of
testing. The major problem with the engine installation was the difficulty of
operating the waste gate. The engine was operating at 38,000 rpm (300 HP) and
the gas forces on the waste gate and exhaust backpressure valve produced all
sorts of queer effects on the foot throttle.
A second problem concerned the use of white gas as a fuel. We had trouble
with vapor lock producing flameouts and no starts. Changing over to JP-4
eliminated these problems and JP-4 was used from then on.
Saturday, April 28th was used to conduct a development program on the
throttle linkage. Various positions of the back pressure valves and systems of
springs and linkages were tried to give the foot throttle the best
"feel" possible. One final system was established which allowed the
driver to operate the foot throttle but it was still not as smooth an operation
as the throttle on a piston engine.
Further testing at the track revealed a further deficiency of the waste gate
system. It was impossible to unload enough horsepower with the waste gate fully
open to prevent the car from coming into the turns too fast.
A change was made here to operate with the gas producer governor alone and
eliminate the waste gate entirely. Acceleration time from idle (15,000 rpm) to
rated (38,000 rpm) was 7 seconds.
Page 3
In a short period of time, the driver (John Zink) learned to anticipate the
power requirements and was turning lap speeds faster than he had ever done with
the waste gate system. During the learning period, he made 15-20 trips into the
field surrounding the track before he found the optimum point at which to stand
on the pedal. Coming on too soon would produce the power before the driver had
the car set up for the straightaway. During this period work was done on the
chassis and suspension to determine optimum spring ratio, shock absorber
setting, sway bar rate, amount of cross weight to be cranked into the
suspension, roll center setting and other items that control the handling in the
turns. This is a difficult process at best since changing any one of the above
influences the others.
The major problem remaining was the engine running out of fuel with about 20
gallons left in the tanks. Relocating the fuel pick up outside on the right hand
tank solved this. This was the last testing to be done prior to leaving for the
Speedway. It was while conducting these tests to determine the minimum amount of
fuel left in the tank before flame out that the accident occurred (May 2nd).
Jack lost it like he’d done many times before but this time, before he had the
car back under control, he hit a small drainage ditch in one corner of the
field. The car rolled over a least once tearing off the right rear wheel
assembly and extensively damaging the chassis and body. Jack suffered a
concussion and facial lacerations and was taken to the hospital. During one
roll, the car landed on the exhaust collector forcing the nozzle ring against
the second stage wheel. The wheel was rubbing when the car was loaded on the
trailer. Following the roll over, there was an oil fire on the nozzle box where
oil had run out of the breather tube. Fortunately there was no fuel fire even
though one fuel tank had been ripped open on top.
There was partial evidence that the foot throttle had been held down during
the accident. The output tachometer tell-tale showed 8000 and both rear axle
half shafts were twisted.
The next four days were spent completely rebuilding the car. All drive line,
steering, and suspension components were magnafluxed. Sections of the frame were
rebuilt and all badly damaged car parts were purchased new.
The engine was disassembled and visually inspected. The only damage was some
metal build up in the nozzle ring wheel shroud where the second stage wheel had
rubbed. This was ground off and the engine reassembled with .017 inch second
stage wheel clearance. The compressor case Marman clamp was damaged and later
replaced.
The car was then checked out on the ranch track late Sunday evening, May 6th,
with Jack again driving. Every thing functioned satisfactorily so the car was
put back on the trailer and delivered to the Indianapolis Speedway.
Page 4
The car arrived Tuesday morning and spent the day going through tech
inspection. Only minor problem was lack of penetrant inspection papers on the
engine. The car got out on the track late in the afternoon and got in three laps
before the track closed down. This was the first time Dan Gurney had seen or
driven the car. During the week of April 28th, Gurney had passed his
drivers test using the John Zink Trackburner No. 72. This is a conventional
roadster with a four cylinder Meyer Drake engine. After passing his test, he
flew to Monaco where he raced a factory Porsche. He arrived back at the Speedway
the same day the turbine arrived.
Gurney’s best time Wednesday with the 300 HP setting was 128 mph. His best
time with the 375 HP setting was 143 mph. This was with a 3.63 rear end ratio.
That night the rear end ratio was dropped to 3.78 and the acceleration time
reduced to 5 seconds (19,000 to 39,000). This failed to produce any decrease in
lap times and it was becoming apparent that Gurney was losing confidence in the
car. He felt that with practice he could pick up another 2 or 3 miles per hour
but that he could never overcome the acceleration lag when driving in traffic.
This conclusion was reached after racing with several other top cars (Troy
Ruttman in the Jim Robbins Special and Eddie Sacks in the Dean Van lines
Special) He then left us to drive a rear engine Buick for Mickey Thompson. He
qualified the Buick at 147 the following Sunday and then left for Holland to
race in the Formula 1 Zandsvort race.
Duane Carter next expressed interest in the turbine. After two days of
practice, Friday and Saturday, he had the car up to 142 mph. Duane is one of the
older more reliable Speedway drivers and was most helpful in comparing the car’s
performance to the conventional roadsters. Although Gurney was faster through
the turns (138 mph versus 128 mph for Duane), Duane’s ability to get back on
the throttle sooner resulted in both drivers turning comparable lap speeds.
Duane’s top speed on the straight was 167 mph versus 155 for Gurney. The Offys
will turn 170-175 mph on the straights.
As it appeared, we had gone as fast as we were going to go without the waste
gate, it was decided to install the linkage so that when the waste gate was
opened, the gas producer would drop back to some predetermined rpm. The setting
for this intermediate rpm was controlled from the dash. The setting generally
ran from 33 to 37,000 rpm, depending on the driver. This of course still left us
with a 1 to 1-1/2 second acceleration lag.
Gurney was prevailed upon to give the turbine one more try but by now he had
been turning qualifying speeds with the Buick and was not too anxious to run the
turbine. He turned a few laps in the 130’s and claimed the waste gate showed
no improvement. He also felt the car was underpowered as evidenced by his lack
of top speed in the straights.
Page 5
Duane drove the car the rest of the day but could only get up to 140 mph
average lap speed, (160 mph top speed). By now it was becoming apparent that the
track temperature was beginning to make itself felt on the engine horsepower.
The temperature along side of the track that day was 98 deg. F.
In order to have a car in the race, Zink put Carter in the Zink roadster that
he qualified at 145.8 mph. As luck would have it, the crankshaft broke halfway
through the last lap dropping his lap speed from 146.8 to 144 mph. With Carter
qualified, we once again had no driver for the turbine.
Monday morning, Bill Cheesbourg stopped by and offered his services in
getting the car up to qualifying speed. Bill had driven the Offenhauser powered
rear engine car built by Zink the year before and is enthused about the future
of rear engine cars at the Speedway. He was under contract to drive the Novi
(supercharged V-8) but the car was in the garage being modified. As it appeared
that the Novi would not be ready in time to attempt a qualification run the
second weekend, Bill spent the next four days driving the turbine. He made a
number of recommendations that improved the speed through the corners.
On Tuesday, he turned in one lap at 145 mph and was consistently turning laps
at 144 mph. The temperature alongside the track that day was 88 deg. F. His top
speed during the 145 mph run was still only 163.
Wednesday and Thursday the temperature rose to 97 deg F and the lap speed
dropped to 143 mph. Bill’s speed through the first and third corners was as
fast as the Offys but his time down the straight away was fully half a second
slower.
Late Thursday, Bill left us to drive the second of the Buicks, which he also
had been checking out during he week. He ran the car into the wall but escaped
unhurt. Before crashing he was turning about 143 mph lap speed.
Thursday night the writer left for Dearborn, Michigan, to give a talk on the
progress of the "Trackburner". The talk was given at the Society of
Automotive Engineers (S.A.E.} Midwest Regional meeting. The talk was apparently
well received and much interest was expressed in the car and proceedings at the
Speedway. Mr. C. L. Bouchard, Manager, Ford Gas Turbine Department took Mr.
Vincent Moore and myself on a tour through their gas turbine facilities before
the meeting.
By now, it appeared that the second Zink car was in danger of being bumped
from the starting line-up so it was decided to give the turbine one more try
with Duane Carter driving. A call to Seattle confirmed the use of another 1000
rpm for the gas producer. That night the gas producer was turned up to 40,000
rpm.
Page 6
Saturday was a scorcher. The temperature in the pits was 105 deg F. The track
temperature was 141 deg F, the highest ever recorded on the Speedway. The inlet
air temperature must have been 115-120 deg F. The best Duane could turn was 143,
lap speed. We did get some times on the car at different sections of the track.
In spite of his low top speed, his elapsed time down the straight way was
comparable to the Offys. His time through turns 1 and 3 were also the equivalent
of the Offys but where he appeared to be losing was through turns 2 and 4. His
times here were about ½ second slower than the Offys. This can only be
attributed to the 1 ½ second acceleration lag. It appears that it’s
impossible for a man to get back on the throttle before the chassis feels secure
in a turn.
Sunday was almost as hot as Saturday so the car remained in the garage and
that was the end of qualifications.
The car made a demonstration run the following weekend at Indianapolis
Raceway Park (not the Speedway) with Henry Banks driving. It was on display at
the Speedway on race day and then returned to Tulsa.
In retrospect, there were three problems that beat us, the acceleration lag,
the heat, and the loss of our original driver. The order or importance is
questionable.
Although no effort was make to silence the engine, the car was much quieter
than the other cars on the track, both to the spectators and driver. Duane
Carter described it as "eerie". He heard the tires patting on the
track and the body creaking and groaning. These were noises he had never heard
in a racecar before.
Both drivers, Cheesbourg and Carter, extolled the virtues of the vibration
free ride. Both drivers wanted to drive the car again in the Milwaukee 100 miler
later in the month.
The engine performed flawlessly. The car ran 270 laps at the Speedway and 370
laps on the 5/8 mile track in Tulsa. This is easily the equivalent of two 500
mile races. Total time on the engine was 9 hours and 150 starts. The EGT ran
1200 deg at Tulsa and 1250 to 1300 degrees at the Speedway. It showed 1350 deg F
when the gas producer was cranked up to 40,000 rpm. We did have a second stage
wheel rub at the Speedway, which was corrected by moving the reduction unit on
the sump and base. We occasionally had trouble with the RH igniter flooding and
not firing. This never happened during a normal start but only during the first
start after we had run out of fuel. The plug was replace but this did not help.
The compressor case Marmon clamp was replaced after the rollover accident.
Outside of this no other engine parts were replaced after the engine left
Boeing. Oil pressure never varied on the turns (40-45 psi), SAE 10 was used in
Tulsa and SAE 20 use at the Speedway. There was a little trouble with oil coming
out of the breather on the turns but this was cured with Chore-Girl stuffed in
the breather.
Page 7
Tire wear was good, 80-90 laps on the right rear and over 150 laps on the
right front and left rear. The left front never was changed. This was not at
competitive speeds so it is only an indication of probable tire wear.
The fuel consumption averaged out at 4.3 miles per gallon. This compares to 3
to 3 ½ for the Offys. The difference between operating with the waste gate or
fuel control was negligible. Brakes also were no problem. In spite of all the
laps on the car, the brake pads were never replaced. The rear pads were worn
less than 25% when the car returned to Tulsa. Wear on the front pads was
negligible.
Everyone was enthusiastic about the car including the other car owners and
drivers. All expressed the opinion that they would like to see the car in the
race. The accessory manufacturers were particularly helpful. Mobile offered to
provide us with any blend or type of fuel or oil that we needed.
When Champion heard we flooded and fouled out one of their igniters, they
flew in their assistant chief engineer along with a variety of igniters to be
tried. Allison had engineers over daily looking over the installation and asking
questions. Allison also helpfully calibrated our tachometer when the readings
became questionable. Don Cummins of Cummins Diesel followed the turbine car
closely as did Lou Meyer, manufacturer of the Offenhauser Racing engine.
In the event that we should run again in "63", there are two basic
changes that would have to be made before the engine can be considered
competitive.
We need 375 HP at 100 deg F inlet air temp. This could be accomplished
with ease using the 5058 axial-radial compressor.
We need a waste gate or pre-whirl that will unload down to a maximum of
20-30 HP while maintaining a constant first stage rpm. The presently used
waste gate was designed for a 175 HP engine. Increasing the by-pass area
would help but there’s still the problem of moving the valves and
linkage without power assistance.
Parallel with engine development would be an improvement in the chassis and
suspension to enable the car to power through turns 2 and 4. This would reduce
the dependence on quick engine response.
The engine will be returned to Boeing at which time it will be disassembled
and inspected to determine the effects of the high operating temperatures on the
hot parts. There are no plans for running the turbine in "63".
Len Williams
Leonard Williams